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Jerking problem #4

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bkubicek opened this issue Aug 25, 2011 · 5 comments
Open

Jerking problem #4

bkubicek opened this issue Aug 25, 2011 · 5 comments

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@bkubicek
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Citation from Joel:

I put a video of my jerking problem on http://www.youtube.com/watch?v=eP-gfCq5mYY
Each movement is 200mm in one axis and 5mm in the other. Speed in gcode was F36000. Once the ratio of each axis exceeds 200mm x 50mm, or the speed gets dropped to F35505, it doesn't jerk

@bradleyf
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Could be related to LCD updates

@jv4779
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jv4779 commented Aug 26, 2011

see https://github.com/jv4779/Marlin/commit/51c423bcf52e7bd594b0cd45830d2e33c7a474e4 that should fix this. Where is the master reposity for Marlin, bkubicek looks to all bout Ultimaker, ErikZalm all about gen6, no response on ErikZalm pull requests, but I can commit here. My pull requests have been issues for all machine variants.

@bradleyf
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jv4779: Pls contact bkubicek and commit it to our experimental branch

@bkubicek
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bkubicek commented Nov 3, 2011

is it still an issue with my current state of the lcd implementation?

@bkubicek
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bkubicek commented Nov 4, 2011

also, did you actually have LCD enabled at all? because otherwise that could never have been an issue.

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3 participants